Now, i hope i don’t offend anyone by this question, but is retiring a locomotive that was involved in a fatal incident out of respect, law, or just some other reason ( such as crew feelings of being in the locomotive that someone was killed in)?
LC
Our thoughts and prayers are with you;
And all of Chris’ family.
I wonder what there going to do to the crew of the Local to bad the line was in DTC blocks hopefully they switch the switch to a Automatic switch so the engineer can check it before it gets their and the engineer would have not died if he went somewhere safe they said he died of breathing the air. they found a tape and the engineer did put the emergancy brake on the NTSB will look at the Black Box tape that the unit had.
Wabash1 I know NS units hav more than 3 didgit numbers I was saying that I don’t know the last numbers the 2nd unit looks like 6598 or 6590,6596 one of those numbers and Augusta is thinking of taking away the street line and replace it somewhere else also the train came though Augusta I would be scared if I saw that train before it wrecked
Did anyone watch ABC news tonight they had something on Dangerous cargo
kevin
Firehouse has several articles about the wreck.
http://cms.firehouse.com/content/article/article.jsp?sectionId=46&id=38077
http://cms.firehouse.com/content/article/article.jsp?sectionId=46&id=38093
http://cms.firehouse.com/content/article/article.jsp?sectionId=46&id=38096
http://cms.firehouse.com/content/article/article.jsp?sectionId=46&id=38080
I think the material on the ground is lading from the hoppers.
ouch brother…sorry to hear that…it realy hits home when its someone you know personaly!!!
csx engineer
I am not 100 percent sure the lead unit will be retired my friend told me that but there was many other units that died but never retired and got the torch like CSX 700 in that unit 3 injures and one death and many other that are still running so I am going to make sure he is not lieing
they are going to patch the tanker sometime tonight and it will be OK then hopefully they clear the whole thing up
kevin
True. I always feel for anyone who is injured or worse, killed on the railroad. I know what it is to have a serious line of duty injury and near death experience all in one, but someone you know is much worse.
Here is a link to todays story about Chris Seeling.
http://www.wistv.com/Global/story.asp?S=2782256
Thanks to everyone for your kind wishes, my prayers are with Chris’ family now.
LC
if that engine is operational it will be put back in service it dont matter if someone died . i did learn it was dark teritory so that brings up 3 other questions. the blame naturally and the ivestigation will go on and on. but here are the problems as i see them
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why did he have a track warrent that allowed him to proceed past a open switch ( os) even rule 99 no flag protection would require the location of that train he hit.
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did the engineer not abide by the tract warrent( no way of knowing as we dont know what he is running on)
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the 2nd most important question is why that switch was left open. I can come up with reasons but until the infomation is in i wont accuse anyone of anything.
these question are that unless you work under the track warrent system you wont understand why i made the statements. and these are general statements and questions not accusing anyone. I hate it that we lost a brother engineer but this is are chosen field, and the system is not perfect. accidents do happen as much as the ns wants to be the safest railroad accidents will happen ( we dont go have on perposes do we) what i am getting at is rule 99 in some way was broken.
that would be a good question for the NTSB
kevin
If somebody is responsible for the open switch, imagine how they are feeling now…
I live less than 30 minutes from Graniteville on the other side of the river in Georgia, so this has been all over the TV. The NTSB spoke at a news conference and stated that the crew of the local were hired back in the 70’s so it’s not like they didn’t know what they were doing. Here’s a question for all the engineers out there, why did they leave the train sitting in the siding of the Avondale Mills plant? They couldn’t bring it back to Augusta which is about 15 minutes or more away? I live less than a mile from CSX’s Spartanburg Subdivision and CSX most always leaves a ballast train sitting in the siding under interstate 20 sometimes for an entire weekend. What is the purpose of leaving trains sitting when they are relatively close to the nearest yard?
My prayers go out the families of both crews and my neighbors in South Carolina.
From my understanding of DTC territory, the train that derailed could not have entered the block that contained the parked train unless that train had cleared up with the dispatcher. I hate to say it, but it looks like the switch is going to be the main focus of the investigation. I’m just hoping that the misaligned switch, if that’s what it is, has nothing to do with the crew. Maybe the switch was picked by a sharp flange???
On CSX in North Carolina a conductor trainee had left a switch lined for a siding in DTC territory that lead to a major derailment. The story of this derailment was posted to make us aware of what can happen when trainees are used as brakemen; they are not to be left out of our sight. I really, really hope the South Carolina incident has nothing to do with this incident, but it kind of echoes what happened. I better just wait for the results to comment more.
QUOTE: Originally posted by oskar
I am not 100 percent sure the lead unit will be retired my friend told me that but there was many other units that died but never retired and got the torch like CSX 700 in that unit 3 injures and one death and many other that are still running so I am going to make sure he is not lieing
they are going to patch the tanker sometime tonight and it will be OK then hopefully they clear the whole thing up
kevin
csx #700 did not get the cutting torch for scrap…it was rebuilt and is back in service…
csx engineer
As a Conductor for the CN, I give you my sympath to you for the losses. I dread that this is one of many gruesome reminders that “hurrying will get you hurt.” No one has EVER been fired for taking the time to do things safely and following the rules. Watch your back guys… I’m feeling positive that there will be a backlash of “efficiency test failures” and the FRA stepping things up to keep things calm. I’m sure glad I took out EXTRA insurance because of the hazards we railroaders face each day.
I appreciate you clearing things up M.W.
Not long ago their was a crossing collision near the derailment site could a family member have something to do with it to get back to NS.
CSXNS - I remember what you are talking about. Not too long ago 4 or 5 employees of Avondale Mills lost there life when they tried to beat a train. I doubt it but you never know what people are capable of these days.
Wabash…I have no knowledge of operations on this line other than what I’ve read since this accident and no clue what is common practice. From the little video clip online of the NTSB spokewoman it sounds like a local crew with one unit was moving some cars around on this spur track approximately 25 cars long. At some point they went off duty and left the locomotive and 2 cars tied down near the mainline. If a crew member of the local left the switch open and perhaps a different member of the crew reported clear of their track warrant (or DTC block authority, not sure of Method of Operation) then the dispatcher is to assume the crew complied with the rules and the switch is returned to normal mainline position. An authority was then rightfully given to the mainline train and they discovered the switch open too late to avoid collision. Another possibility is that the dispatcher was informed the switch was left open and then he should have instructed the mainline crew to restore the switch to normal position before passing said location. Dispatchers can fail to protect against switches left open. Train crews can also fail to abide by instructions in their authorities. Yet another possibility is that someone besides the local crew lined the switch into the spur track. As for the chances of the switch points picking a flange…it is possible but unlikely. Typically a flange within the train is picked and a derailment follows. Another possibility is that the switch was defective due to it being run thru in the trailing position…another lesser likely culprit.
New York Times article states the switch was lined for the siding and locked into position. It also states the FBI took part of the switch to analize the fingerprints.